MEC&F Expert Engineers : Probable cause of the deadly crash of CESSNA T207A, registration: N7311U plane in Paze, Arizona

Wednesday, July 8, 2015

Probable cause of the deadly crash of CESSNA T207A, registration: N7311U plane in Paze, Arizona

 


 
NTSB Identification: WPR14FA186
14 CFR Part 91: General Aviation
Accident occurred Saturday, May 10, 2014 in Page, AZ
Probable Cause Approval Date: 06/18/2015
Aircraft: CESSNA T207A, registration: N7311U
Injuries: 1 Fatal, 1 Serious, 5 Minor.
 
NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

During a local sightseeing flight, the pilot noticed that the engine had lost partial power, and he initiated a turn back toward the airport while troubleshooting the loss of power.

Despite the pilot’s attempts, the engine would not regain full power and was surging and sputtering randomly. The pilot entered the airport’s traffic pattern on the downwind leg, and, while on final approach to the runway, the airplane encountered multiple downdrafts and wind gusts.

It is likely that, due to the downdrafts and the partial loss of engine power, the pilot was not able to maintain airplane control. The airplane subsequently landed hard short of the runway surface and nosed over, coming to rest inverted.

The reported wind conditions around the time of the accident varied between 20 and 70 degrees right of the runway heading and were 14 knots gusting to greater than 20 knots.

In addition, a company pilot who landed about 8 minutes before the accident reported that he encountered strong downdrafts and windshear while on final approach to the runway and that he would not have been able to reach the runway if he had a partial or total loss of engine power.

Postaccident examination of the airframe and engine revealed no evidence of any preexisting mechanical malfunctions or failures that would have precluded normal operation. The engine was subsequently installed on a test stand and was successfully run through various power settings for several minutes. The reason for the partial loss of engine power could not be determined.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:  


The pilot’s inability to maintain aircraft control due to a partial loss of engine power and an encounter with downdrafts and gusting crosswinds while on final approach to the runway. The reason for the partial loss of engine power could not be determined because postaccident examination revealed no mechanical malfunction or failure that would have precluded normal operation.